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View Full Version : My progress...Part Deux!


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JET
09-07-2005, 09:23 PM
Well I just got back from the dyno and it didn't go exactly as planned.

The good news is that it went better than last time!! The first thing was some crap gas. They must have the refineries cranked up and are putting out some crappy gas, or I just happened to get crap gas (holiday 93). There was also an issue with boost creep. The wastegate hole in the PTE housing must not be big enough. I am going to have to take that off and port it out. I ended up making 397whp at 5200 rpm (had to let off because of creep) on pump gas. The power was climbing really good and mid to upper 400's should be obtainable on pump.

Put 10 gal of 111 (Steve Hill pump gas :D ) in so we could ignore the boost creep and get some more RPM out of it. The AEM was set to shut off if the boost hit 25 psi, this happened at 6300 RPM and it made 455 whp. Power was still climbing good, but there was a blurp of coolant when Shane let off. Rut roh. I hadn't retorqued the head studs, so I did that. Made one more run, but it didn't help and blew coolant.

There were a few loose nuts on the one end. I never checked the head when I got it back from the machine shop either. It could be machined wrong. I will pull the head off and check things out. Even short shifting at 5500 RPM, it was a run drive home. I got on it a couple of times once I was getting close to home. She was running low on coolant when I pulled onto my street :D At least I didn't start any fires this time!!

AJ
09-07-2005, 09:42 PM
Well nice numbers considering... It sucks you have to go about taking the head off. Think it's just a minor HG issue now?

niterydr
09-07-2005, 10:00 PM
How many pulls did you make on the dyno?

JET
09-07-2005, 11:03 PM
We probably made 8-10 full pulls on the dyno (til boost cut). There was a bunch of midrange tuning that Shane did too. Only 2 pulls on 111 though.

AJ- Hopefully it is just the headgasket. If Wag's fucked up I am going to be pissed. It is decked so far that it will be junk (their fault), but with 18 hours of porting in it and machined for 1mm oversized valves. If I bust ass I can probably swap the HG in 2 hours, so that isn't a biggie. Yanking the turbo shouldn't be too bad either.

rk4g63
09-07-2005, 11:27 PM
Is the head a 3 angle job?

JET
09-08-2005, 12:24 AM
Basically all heads done now are 3 angle. This one was supposed to be a 5 angle, but is probably 3.

Jakey
09-08-2005, 12:37 AM
What brand of valves are you running JET?

JET
09-08-2005, 01:04 AM
Nitride coated SI's, 1mm over.

JET
09-12-2005, 12:39 AM
Well, the turbo has the WG ported out more to stop the boost creep. The head is back on with a Cometic head gasket. I just have to put the turbo on, timing belt stuff and hook everything up. It will be running tomorrow afternoon again. Just in time for me to leave for the week.

Shotgun!
09-12-2005, 12:47 AM
:thumpsup: