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Old 02-02-2011   #1
notsostockgalant
3g camaro owner
 

Join Date: May 2009
Location: Plato, MN
Drives: 88' camaro 400hp 327 sbc
Posts: 155
Re: 95 Tsi Awd PPPPPProject

Got er fixed up last week for the most part.

Slave was leaking from the crush washers on the line.






Axle hanger came loose, causing the boot to come partially off.(dont mind the oil its just from the power steering loop leaking, I plan to pull the rack when the tie rod ends get replaced here soon)






Heres a pretty awesome heat mark on the front and back of the flywheel in the same spot.





Heres the whole reason it came back out, last 2 pics are centered on my old fidanza starter ring.









Clutch disk looked good as did the pressure plate, scuffed em with some 400 grit and put em in with the fidanza.



Being that the fidanza was used, I rolled around it with a 60grit 3M ROLOC disc on a pneumatic sander a few times to make sure there weren't any gouges/groves/unseen high/low spots in it, followed by a 100grit surfacing pad which left it with a nice smooth level finish. Wish I would have taken some pics of this......

Car Shifts better than it ever has since the clutch disengages with one push of the pedal and not 25 pumps haha.

Last edited by notsostockgalant; 02-02-2011 at 11:24 PM..
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Old 02-02-2011   #2
notsostockgalant
3g camaro owner
 

Join Date: May 2009
Location: Plato, MN
Drives: 88' camaro 400hp 327 sbc
Posts: 155
Re: 95 Tsi Awd PPPPPProject

Heres some more turbo trivia...





78-11830

and I checked right near the flange towards the CHRA and there is indeed an 070 so its a 7cm turbine housing aswell, forgot to take note of the other numbers though.

Couple front shots



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Old 02-02-2011   #3
notsostockgalant
3g camaro owner
 

Join Date: May 2009
Location: Plato, MN
Drives: 88' camaro 400hp 327 sbc
Posts: 155
Re: 95 Tsi Awd PPPPPProject

The car shifted awesome, and the creep issue was fixed after I noticed that the WG flapper arm coming off of the turbine housing had gotten bent somehow....... After straightening that out, I was only getting about 3lbs of creep with the boost controller set at 10 lbs,so I set it to 15lbs and it held just fine all the way to redline.
Then on friday

Then on friday I was having some issues with my stock Radiator leaking, come to find out the plastic separated from the aluminum.

So I fitted up a civic radiator I had laying around.( the fins are pretty rotten/non existent in most spots, but the tubes and endtanks are solid)







I had to temporarily JB weld the upper and lower neck from the Talon radiator onto the civic one for the time being, because the Honda rad uses smaller hoses.(I bought some adapters and removed the jbwelded ends on Monday)




I plan to get an aluminum Honda/half size radiator, then I'll just weld the correct size upper and lower necks onto it.



After swapping in the adapters on monday I went for a test spin and it blew the upper radiator hose, so I put it back on and went out for test run#2 and attempted to make a 3rd gear pull ,well the temp went from 180 to 215.

Let it cool down all the way, pulled the rad cap and fired it up......
Bubbles....... but once the car warmed up it stopped bubbling.

So, the heads comin off sooner than later, seems the oil leak that ran along the headgasket was not from the intake came seal since it has gotten alot worse aswell, the cars fine as long as you stay out of boost, but whats the fun in that.

Last edited by notsostockgalant; 02-03-2011 at 12:01 AM..
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