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1ViciousGSX
12-11-2007, 12:03 PM
Are these the three you are talking about?

1. Straight from battery to firewall, just a few inches long
2. From battery down to transmission, hooks on with one of the starter bolts
3. Intake mani to firewall
Yes

Kevin 1G Drummer
12-11-2007, 05:27 PM
There's also one more from the transmission to the frame rail. At least there is on mine.

Kracka
12-11-2007, 05:31 PM
There's also one more from the transmission to the frame rail. At least there is on mine.

Yup.

asshanson
12-11-2007, 11:33 PM
Worked on it quite a bit today, and everything was going slow as usual so I didn't get done everything I wanted to.

However, the front wheel assemblies are all put together except for the center nut thingy, which is like 30mm and I don't have a socket that big, but I should have one tomorrow.

Also, I spent like an hour dealing with these stupid studs on the intake mani. They are an inch longer than the usual length and it took FOREVER to get them off. It took three nuts together as tight as I could, and a couple tries with that to get them broken loose. These are the stupid little problems I've been dealing with the entire process.

b00stcreep21
12-11-2007, 11:44 PM
The axle nuts are 32mm's

A//// Guy
12-12-2007, 09:10 AM
Worked on it quite a bit today, and everything was going slow as usual so I didn't get done everything I wanted to.

However, the front wheel assemblies are all put together except for the center nut thingy, which is like 30mm and I don't have a socket that big, but I should have one tomorrow.

Also, I spent like an hour dealing with these stupid studs on the intake mani. They are an inch longer than the usual length and it took FOREVER to get them off. It took three nuts together as tight as I could, and a couple tries with that to get them broken loose. These are the stupid little problems I've been dealing with the entire process.

So whats left? Also did you find the harness, and the banjo bolt yet? Also call map about tranny fluid.

asshanson
12-12-2007, 01:59 PM
The IC pipes and radiator are left still, but I'll probably get those done tonight after work. After that it's pretty much just getting the fluids in, wiring the CAS harness (which I hope to find in the junkyard after work), and getting the banjo bolt for the oil feed line.

I have a question though, about the power transistor unit, I think that's what it's called. When reading through the Magnus tutorial about the 6 bolt swap, it said to use the 2g power transistor with a custom mounting bracket. I see that there is no spot on the 1g intake mani to mount it, and the 1g coil pack doesn't have a spot for it either. What exactly is this part, and can I just ziptie it securely to something? Why was it mounted to the 2g coil pack originally? Just for fun, or does it have to have an electrical connection to it?

scheides
12-12-2007, 02:21 PM
blageo made a nice mount for his to go on his intake manifold, I don't remember where mine was. If nothing else, make sure the metal part is grounded, as I think those get fairly hot and need to dissipate heat.

crazy_skier
12-13-2007, 12:17 AM
thats some great progress... post up some pics when its all said and done

asshanson
12-17-2007, 12:01 AM
ITS ALIVE!!!!!!!!!!!!!!

I can't even begin to describe my happiness right now, it's so great to be able to drive my car again, after 2 solid months without it. HUGE thanks to Peter for driving down here and helping it get put 100% back together, was a good weekend of work/bar time.

There were a few major issues at the end of the process, and some aren't completely worked out yet, but it drives. Here's a list of the outstanding issues:

1. Throttle cable or throttle body isn't setup right, maybe TPS sensor isn't setup right either (I used my 2g tps). At first the throttle body/cable was sticky and when we were first driving the throttle got stuck open at like 10%. We used some PB blaster to loosen it up and it seems to work better now, I took it for another spin around Des Moines and the throttle goes back to .1 or .2 % now. Not 0%, but close enough for me to drive back home.

2. Car idles oddly, BISS screw is all the way in, and I can't find any super obvious air leaks in the intake. When cold it idles at 1800, then warms up and goes down to 1400rpm, and sometimes dip to 1000 quickly, then back. Maybe related to the throttle body issues. I used my 2g ISC, so that shouldn't be the issue.

3. Logger doesn't work since the palm battery died and I'm sure it lost the program from memory, so I have to wait until I get back to start logging. Which means I can't set the Cam Angle Sensor. I have it set to the middle of the adjustment for now, so it's at unknown base timing for now. I'm not going to get into boost until I get these issues fixed, so I should be safe.

4. Coolant is leaking very slowly from the water neck where the line goes to the overflow bottle. I'm going to replace the radiator cap when I get back and get a real hose clamp to tighten the overflow line instead of the metal clip on there now.

5. Starter is acting up sometimes. It seems to try starting for a second normally, and then the starter seems to spin freely, just makes a high pitch whining. I try to start again and it starts right up within 1 second. What could cause this?

That's all I can think of for now, I'm just happy it turned on without any real problems. Here's some of the other things we ran into:

1. 1G CAS harness to 2g plugs adapter from Magnus didn't get overnighted, even though I paid the $55 extra for it. In the end I just custom made one which is ghetto, but works for now. The real one should arrive tomorrow, I'll try to get my shipping refunded.

2. Clutch adjustment screw wasn't set right for the 2900. It scared me bad, because we finally got it working, and I tried to get it in gear and it wouldn't disengage the clutch, luckily I adjusted it and it works now. I don't mind the 2900 that much at all, I don't know what people complain about, maybe it'll get annoying after awhile.

3. Lower radiator pipe had to be rigged up below the LICP since there is a stupid counter weight on the transmission blocking that route for the pipe.

I'm tired now, going to bed.