MitsuStyle MitsuStyle

Go Back   MitsuStyle > Tech > Turbo / Engine / Drivetrain

 
 
Thread Tools Display Modes
Prev Previous Post   Next Post Next
Old 03-06-2005   #40
john
Business as usual
 
john's Avatar
 

Join Date: Oct 2003
Location: Isanti, MN
Drives: Dodge Viper and Honda Insight
Posts: 2,206
Re: problem

No, it is just that several things went wrong at the same time. Had "phantom valve bend" on the ported head, a head with crappy compression, the 2g head finally back on. Then no spark twice and spark and fuel without starting. Everything was going wrong and I did not have any time or will to help him with the car after swapping the head, intake mani, etc for the third time. After swapping it three times, the car ended up with the head that was on it originally instead of an upgraded 1g.
__________________
97 Viper GTS
03 Mercedes CLK500 rollin on dubs...
john is offline   Reply With Quote
 

Thread Tools
Display Modes

Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off



All times are GMT -5. The time now is 09:31 PM.


Powered by vBulletin® Version 3.8.4
Copyright ©2000 - 2025, Jelsoft Enterprises Ltd.