Quote:
Originally Posted by Mark Leasure
Did you get it back together this weekend?
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Hell yea! JUST got back from ripping around the neighborhood. Total, about 4 hours apart, couple hours (ok like 4) of cleaning and getting parts run around, maybe about 6 hours to get it back together. I made a few boneheaded mistakes but hey I caught them before it was too late
Yanked the cams to bolt the head to the block (dumb design imho but whatever):
Freshy fresh:
found a few nicks in the headgasket I got, not sure if that was from me or mitsu or what but I sure wish they would put these things in cardboard packaging, would be worth the extra $5 cost imho
I cleaned it up as best I could and used it anyways, it looks worse than it is I think.
gasket on, head bolted down, cams bolted in, gears on, timing chain mounted and timing set, chain tensioner set(this was one of my oopsies, put it in but forgot to tighten the bolts! doh!), and timing cover cleaned, RTV'd, installed, uninstalled, re-rtv'd, and re-installed
More freshy-fresh parts! I put in the revised timing chain from the 2010's:
New on the left (mounted), old one on the right:
After all the belt problems I had, bought a new tensioner and pulley. The pulley was like $65 and the tensioner + pulley was only like $30 more so I just got the whole assembly (still plastic but goes nice with my nice metal hyundai pulleys!)
So that's about it! Fired right up, no leaks yet, changed oil, fresh coolant, ripped it around the block a few times and parked it. Undertray, heat shields, and strut tower go back on tomorrow and it's back to DD duty for this pig. Car still sounds kinda diesely on cold start (but it always has a little) so its part injectors and maybe the rings on #1 are part of the problem. I'll just check the oil every 100 miles (as I have been all fall) and see what happens. Gonna check logs (did some quick pulls but with all the snow there's no traction!) and drink a beer.
THANK YOU EVERYONE FOR YOUR INPUT! Thank you MAP for the parts and coordinating with Wagemon Bros machine shop, total downtime was only *three* days, not bad!