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Old 02-06-2010   #5
Eurotrash
 

Join Date: Dec 2009
Location: Rosemount
Drives: 92 Laser RS
Posts: 36
Re: Strange mis-fire problem

Quote:
Originally Posted by 4g63tcrazy View Post
I can't believe after he admits a coupler is loose and he hasnt done a boost leak test people are suggesting other things.. Also just cause your boost controller is turned down doesn't mean your not running any boost. Can't expect your car to run good if it thinks its getting a lot more air then what it's actually getting. Do a boost leak test and go from there.

Indeed, the car was still making boost which was not good because i'm still breaking in the engine. however, with the couplers tight the problem was less severe. So that was part of the issue. Car NEEDS a tune and a new MAF. Which I'm a newbie with dsm's, so im not sure what to do about a MAF. Seems people run different MAF's. Question is, do i get a stock 1G, a stock 2G, or this 3" GM one people are using? What would i need to use the 2G or the GM one? Thanks for bearing with me guys.. I'm used to VW's, So this is an entire new world to me
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