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Re: Make slowboy not so slow
ITS ALIVE!!!!!!!!!!!!!!
I can't even begin to describe my happiness right now, it's so great to be able to drive my car again, after 2 solid months without it. HUGE thanks to Peter for driving down here and helping it get put 100% back together, was a good weekend of work/bar time.
There were a few major issues at the end of the process, and some aren't completely worked out yet, but it drives. Here's a list of the outstanding issues:
1. Throttle cable or throttle body isn't setup right, maybe TPS sensor isn't setup right either (I used my 2g tps). At first the throttle body/cable was sticky and when we were first driving the throttle got stuck open at like 10%. We used some PB blaster to loosen it up and it seems to work better now, I took it for another spin around Des Moines and the throttle goes back to .1 or .2 % now. Not 0%, but close enough for me to drive back home.
2. Car idles oddly, BISS screw is all the way in, and I can't find any super obvious air leaks in the intake. When cold it idles at 1800, then warms up and goes down to 1400rpm, and sometimes dip to 1000 quickly, then back. Maybe related to the throttle body issues. I used my 2g ISC, so that shouldn't be the issue.
3. Logger doesn't work since the palm battery died and I'm sure it lost the program from memory, so I have to wait until I get back to start logging. Which means I can't set the Cam Angle Sensor. I have it set to the middle of the adjustment for now, so it's at unknown base timing for now. I'm not going to get into boost until I get these issues fixed, so I should be safe.
4. Coolant is leaking very slowly from the water neck where the line goes to the overflow bottle. I'm going to replace the radiator cap when I get back and get a real hose clamp to tighten the overflow line instead of the metal clip on there now.
5. Starter is acting up sometimes. It seems to try starting for a second normally, and then the starter seems to spin freely, just makes a high pitch whining. I try to start again and it starts right up within 1 second. What could cause this?
That's all I can think of for now, I'm just happy it turned on without any real problems. Here's some of the other things we ran into:
1. 1G CAS harness to 2g plugs adapter from Magnus didn't get overnighted, even though I paid the $55 extra for it. In the end I just custom made one which is ghetto, but works for now. The real one should arrive tomorrow, I'll try to get my shipping refunded.
2. Clutch adjustment screw wasn't set right for the 2900. It scared me bad, because we finally got it working, and I tried to get it in gear and it wouldn't disengage the clutch, luckily I adjusted it and it works now. I don't mind the 2900 that much at all, I don't know what people complain about, maybe it'll get annoying after awhile.
3. Lower radiator pipe had to be rigged up below the LICP since there is a stupid counter weight on the transmission blocking that route for the pipe.
I'm tired now, going to bed.
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