SlowWhite
01-27-2006, 10:05 PM
Well tonight was an up and down night. Hit a new personal best MPH but that's about it.
Save alot of time here's the overview. - 3 trips down the track (and all the tuning I could get during those 3 trips)
Ended up getting me from 12.3@116mph to an
r/t =.788
60 - 1.960
330 = 5.243
1/8 = 7.846
mph = 96.72
1000 = 10.028
1/4 = 11.881
mph = 120.49
After that it was down hill. - next run I turned the boost up less then 1/4 turn and it went from 28psi - 35psi and had a really bad run gave up after having to shift back into 1st gear ran a 15 something
I changed spark plugs lowered the boost - and then tried again ended up running another 15 something after wheel hooping really badly. Somethings up now the car drove fine all the way home, shifts into all the gears just fine. But I noticed when trying to turn into my garage the car felt like it was binding.
I jacked the car up and noticed the front wheels spun a little bit (might have been tension in the AWD drivetrain) Anyrate and then did a boost leak test just to see if it was a blown coupler or something. Nope my Magnus SMI has a major leak in it. I haven't pin pointed it yet as it's coming from bottom side of the SMI. I think a weld might have broke or something. The #1 running already had a pin sized whole in it so maybe another weld was bad. It sounds like it's coming from the #3 runner. But like I said I haven't had the chance to put a light on it yet or really give the car a good once over.
Anyrate my 11.88 run was I'm pretty sure 30psi dropping to 28psi 116oct and about 54lbs/min.
Save alot of time here's the overview. - 3 trips down the track (and all the tuning I could get during those 3 trips)
Ended up getting me from 12.3@116mph to an
r/t =.788
60 - 1.960
330 = 5.243
1/8 = 7.846
mph = 96.72
1000 = 10.028
1/4 = 11.881
mph = 120.49
After that it was down hill. - next run I turned the boost up less then 1/4 turn and it went from 28psi - 35psi and had a really bad run gave up after having to shift back into 1st gear ran a 15 something
I changed spark plugs lowered the boost - and then tried again ended up running another 15 something after wheel hooping really badly. Somethings up now the car drove fine all the way home, shifts into all the gears just fine. But I noticed when trying to turn into my garage the car felt like it was binding.
I jacked the car up and noticed the front wheels spun a little bit (might have been tension in the AWD drivetrain) Anyrate and then did a boost leak test just to see if it was a blown coupler or something. Nope my Magnus SMI has a major leak in it. I haven't pin pointed it yet as it's coming from bottom side of the SMI. I think a weld might have broke or something. The #1 running already had a pin sized whole in it so maybe another weld was bad. It sounds like it's coming from the #3 runner. But like I said I haven't had the chance to put a light on it yet or really give the car a good once over.
Anyrate my 11.88 run was I'm pretty sure 30psi dropping to 28psi 116oct and about 54lbs/min.